Still managed to get a couple small mechanical tasks done on the build today. Also thanks to the trouble shooting help of David and Ken, I was able to finally solve the servo travel issue for the forward planes using the Depth Cruiser module.
After figuring out where I went wrong with the DC module set up, I decided to design and build a set of telescoping double universal joints similar to the solid versions that I made the other day. Simple, quick and dirty.
Nothing fancy.
Set made and finished. Time to install.
Fit just like the solid non telescoping versions did. These were probably not necessary but it gives some freedom of play in the driveline.
Here’s a link to a short video of the motors running with the new universals.
Nick

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